I've resisted it for as long as I possibly could but I can no longer do so.
Effective January 1, 2026, the labor rate will be 125.00 dollars per hour. All work that comes in after that date will be billed at the new rate.
Lititz, PA 717-626-4226 Dewey@VicknairRestorations.com
I've resisted it for as long as I possibly could but I can no longer do so.
Effective January 1, 2026, the labor rate will be 125.00 dollars per hour. All work that comes in after that date will be billed at the new rate.
Here's an AyA No.2 with a few problems. The first of these are cracks at the stock horns, the second is a broken striker, the cause of which will be covered in that segment of the post and, finally, a faulty ejector mechanism, caused by half-assed "gunsmithing". Let's dive right in...
The cracks at the head/horns that made their way to the rear of the lockplates...
The stock and forend were stripped and de-oiled in preparation for repairs and refinishing. After repairing the cracks, the pull length was adjusted to the client's specification. A new buttplate and screws were also made to match his other AyA's original black plastic buttplate. The stock and forend were then refinished and the checkering recut.With the wood finished, I turned my attention to the ejector mechanism. As you can see in the photos, the right-side ejector tumbler had been welded, in an attempt to build up the trip surface. Beside being crudely done, the weld "repair" would have a very short lifespan (as is obvious from the below photo), so a new tumbler was made from 01. After disassembly, I discovered that the dipshit had also welded on the right-side ejector mainspring, rendering it useless as well. A new spring was made from 1095.The finished new parts, alongside the damaged originals...There are many words that one could use to describe the gunsmithing "industry" (not really an industry at all). Words like witchcraft, ignorance, hubris, craftsmanship (ha!, just kidding) but the most fitting might just be... incompetence.
I know of no other line of work where, so often, actual science is simply ignored, if not disbelieved outright.
Physics, chemistry, materials science, basic arithmetic, these apparently hold no sway at the bench of the "gunsmith", who believes that his knowledge is actually that.
One of the most common misconceptions among these practitioners (and also among many end-users) is that a loose rib can be correctly repaired without a complete strip and relay. This is not so. The reasons why are described in detail elsewhere on this blog. That being the case, I won't reiterate it here but I will show yet another example of why anyone that says otherwise should be viewed with suspicion regarding their abilities.
In the case of the end-user (the customer), this belief can be forgiven because he or she can't realistically be expected to know about such things. In the case of anyone calling themself a gunsmith, it is wholly unforgivable.
Here is what was once a Westley Richards Hand Detachable in 16 gauge, with 30 inch barrels. It was the victim of exactly the kind of partial "repair" against which I have railed for as long as I can remember. What is worse, is that the perpetrator should have known better, given their reputation. They are now out of business, so maybe their reputation wasn't so deserved.
Doing it right, the first time, is always not only cheaper, the results will also last a lot longer.
Yet another fine example of a beautifully made gun damaged by so-called "professionals". As always, I won't mention any names (you'd know them and probably wouldn't believe me anyway).
It came in with: a failed ejector spring, a failed mainspring, sears that would not hold the hammers cocked, damaged screws and some of the worst stock modification and finishing I'd ever seen. The failed springs were no one's fault but that can't be said for the rest of the damage.
The right-side hammer pivot screw was damaged. Since this damage would hinder the hammer's proper movement, it was the first item that needed to be corrected. I made (from O1), fitted and engraved the new screw, then heat-treated and finished it to match the frame. With this done, I could move on to correcting the situation with the sears, which we will come to presently.